标签:http lis github speed pat sig lob *** pue
/********************************************************************** * I.MX6 KEY_ROW4 can‘t as GPIO pin * 说明: * Tony遇到KEY_ROW4作为GPIO口时无法设置高、低电平问题,后来通过在 * 相关patch中找到方法,很特殊。 * * 2016-11-26 深圳 南山平山村 曾剑锋 *********************************************************************/ 一、参考文档: 1. android-imx6-kitkat/kernel_imx.git/3.0.35/SR-0013-Split-C1-to-C1-and-microsom.patch https://github.com/rabeeh/android-imx6-kitkat/blob/master/kernel_imx.git/3.0.35/SR-0013-Split-C1-to-C1-and-microsom.patch 2. [meta-freescale] [PATCH] Added support for the SolidRun HummingBird (also known as Carrier One) https://lists.yoctoproject.org/pipermail/meta-freescale/2014-January/006271.html 二、解决方法: #define MX6DL_ENET_PAD_CTRL_PD (PAD_CTL_PKE | PAD_CTL_PUE | \ PAD_CTL_PUS_100K_DOWN | PAD_CTL_SPEED_MED | PAD_CTL_DSE_40ohm | PAD_CTL_HYS) IOMUX_PAD(0x0650, 0x0268, 5, 0x0000, 0, MX6DL_ENET_PAD_CTRL_PD), /* KEY_ROW4 reset signal */
I.MX6 KEY_ROW4 can't as GPIO pin
标签:http lis github speed pat sig lob *** pue
原文地址:http://www.cnblogs.com/zengjfgit/p/6104827.html